{"id":2186,"date":"2020-09-17T22:46:47","date_gmt":"2020-09-17T21:46:47","guid":{"rendered":"https:\/\/www.missendenrailwaymodellers.org.uk\/?page_id=2186"},"modified":"2020-10-16T21:44:01","modified_gmt":"2020-10-16T20:44:01","slug":"virtual-missenden-wifi-controlled-bedford","status":"publish","type":"page","link":"https:\/\/www.missendenrailwaymodellers.org.uk\/index.php\/virtual-missenden-wifi-controlled-bedford\/","title":{"rendered":"Virtual Missenden &#8211; WiFi Controlled Bedford"},"content":{"rendered":"\n<p>A prototype project to create a WiFi controlled Bedford QLD lorry in 4mm scale.<\/p>\n<div class='white' style='background:rgba(0,0,0,0); border:solid 0px rgba(0,0,0,0); border-radius:0px; padding:0px 0px 0px 0px;'>\n<div id='slider_2168' class='owl-carousel sa_owl_theme owl-pagination-true autohide-arrows' data-slider-id='slider_2168' style='visibility:hidden;'>\n<div id='slider_2168_slide01' class='sa_hover_container' style='padding:5% 5%; margin:0px 0%; min-height:300px; '><h4 style=\"text-align: center;\">Requirement<\/h4>\r\n<p>The purpose of this project is to create a motor vehicle that can be loaded and unloaded from a flat wagon. The requirement was simply to be able to drive it backwards and forwards at a controllable speed. On the layout it was due to be used on it would emerge from a building, drive along a loading dock onto a waiting flat wagon or Loriet. Since it only had to drive in a straight line no steering facility was required.<\/p><\/div>\n<div id='slider_2168_slide02' class='sa_hover_container' style='padding:5% 5%; margin:0px 0%; min-height:300px; '><h4 style=\"text-align: center;\">The vehicle<\/h4>\r\n<p>Rather than build a kit or scratch build a vehicle it was decided to start with an off the shelf model and do the necessary modifications to motorise it. The vehicle chosen as an Oxford Diecast Bedford QLD in RAF livery. The layout it was destined for being set in 1944\/45.<\/p>\r\n<p><img decoding=\"async\" class=\"aligncenter wp-image-2179 size-medium\" src=\"https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/76QLD007_1024x1024-300x226.jpg\" alt=\"76QLD007_1024x1024\" width=\"300\" height=\"226\" srcset=\"https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/76QLD007_1024x1024-300x226.jpg 300w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/76QLD007_1024x1024-768x579.jpg 768w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/76QLD007_1024x1024.jpg 1000w\" sizes=\"(max-width: 300px) 100vw, 300px\" \/><\/p><\/div>\n<div id='slider_2168_slide03' class='sa_hover_container' style='padding:5% 5%; margin:0px 0%; min-height:300px; '><h4 style=\"text-align: center;\">The Plan<\/h4>\r\n<p>As far as possible I wanted to use off the shelf components; both for the drive mechanism and the electronics. I already had some experience using the little ESP8266 processors that have built in WiFi and knew they worked well and would fit in the back of the Bedford. This would allow me to control the vehicle speed and direction using a WiFi connection. A standard size board called a WeMOS board would give me what I wanted.<\/p>\r\n<p><img decoding=\"async\" class=\"size-medium wp-image-2180 aligncenter\" src=\"https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/D1_MINI_01_NEU-300x300.jpg\" alt=\"D1_MINI_01_NEU\" width=\"300\" height=\"300\" srcset=\"https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/D1_MINI_01_NEU.jpg 300w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/D1_MINI_01_NEU-150x150.jpg 150w\" sizes=\"(max-width: 300px) 100vw, 300px\" \/><\/p><\/div>\n<div id='slider_2168_slide04' class='sa_hover_container' style='padding:5% 5%; margin:0px 0%; min-height:300px; '><h4 style=\"text-align: center;\">The Motor\/Gearbox<\/h4>\r\n<p>I needed a motor and gearbox that was small enough to fit between the chassis rails of the Bedford, yet with a high enough gear ratio not to result in a lorry capable of breaking the land speed record. Fortunately, after some time searching I found exactly what I needed on an internet site in Poland.\u00a0<\/p>\r\n<p><img decoding=\"async\" class=\"size-medium wp-image-2191 alignleft\" src=\"https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/IMG_2648-300x258.jpg\" alt=\"IMG_2648\" width=\"300\" height=\"258\" srcset=\"https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/IMG_2648-300x258.jpg 300w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/IMG_2648-1024x880.jpg 1024w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/IMG_2648-768x660.jpg 768w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/IMG_2648.jpg 1479w\" sizes=\"(max-width: 300px) 100vw, 300px\" \/>This motor\/gearbox is very small, the gearbox is just 6.2mm wide, however it still manages a 2016 to 1 gear ratio. This should give me good low speed running.<\/p>\r\n<p>The axle are 1mm diameter and will need sleeving to take the original wheels.<\/p><\/div>\n<div id='slider_2168_slide05' class='sa_hover_container' style='padding:5% 5%; margin:0px 0%; min-height:300px; '><h4 style=\"text-align: center;\">Motor Interface<\/h4>\r\n<p>An H-Bridge device would allow two outputs from the processor to control the direction. By pulsing the outputs I could use PWM to control the speed of the motor. Small H-bridge breakout boards are readily available on well known internet auction sites.<\/p>\r\n<p><img decoding=\"async\" class=\"alignleft wp-image-2181\" src=\"https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/s-l1600-2-300x300.jpg\" alt=\"s-l1600-2\" width=\"200\" height=\"200\" srcset=\"https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/s-l1600-2-300x300.jpg 300w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/s-l1600-2-150x150.jpg 150w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/s-l1600-2-768x768.jpg 768w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/s-l1600-2.jpg 1002w\" sizes=\"(max-width: 200px) 100vw, 200px\" \/>This device is actually a dual H-Bridge that can run two motors, we will however only be using half of the device.<\/p><\/div>\n<div id='slider_2168_slide06' class='sa_hover_container' style='padding:5% 5%; margin:0px 0%; min-height:300px; '><h4 style=\"text-align: center;\">Power Supply<\/h4>\r\n<p><img decoding=\"async\" class=\"alignright wp-image-2183\" src=\"https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/s-l1600-4-300x300.jpg\" alt=\"s-l1600-4\" width=\"200\" height=\"200\" srcset=\"https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/s-l1600-4-300x300.jpg 300w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/s-l1600-4-150x150.jpg 150w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/s-l1600-4-768x768.jpg 768w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/s-l1600-4.jpg 1000w\" sizes=\"(max-width: 200px) 100vw, 200px\" \/>The WeMOS board can accept 5 volts and produces the 3.3 volts needed by the processor. This 3.3 volts would also work well for the motor\/gearbox combination. Another board in the WeMOS range is a battery controller for LiPro batteries. These batteries must be used with care and must never be completely discharge. The controller board manages this and provides a charging circuit also.<\/p>\r\n<p>&nbsp;<\/p>\r\n<p>&nbsp;<\/p>\r\n<p><!--nextpage--><\/p>\r\n<p><img decoding=\"async\" class=\"alignleft wp-image-2182 size-medium\" src=\"https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/s-l1600-300x300.jpg\" alt=\"s-l1600\" width=\"300\" height=\"300\" srcset=\"https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/s-l1600-300x300.jpg 300w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/s-l1600-1024x1020.jpg 1024w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/s-l1600-150x150.jpg 150w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/s-l1600-768x765.jpg 768w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/s-l1600-1536x1529.jpg 1536w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/s-l1600.jpg 1600w\" sizes=\"(max-width: 300px) 100vw, 300px\" \/>Searching again on the same well known internet auction site I have a small LiPro battery designed to fit into one of the small drones that are available today. It is a perfect fit for my chosen lorry.<\/p><\/div>\n<div id='slider_2168_slide07' class='sa_hover_container' style='padding:5% 5%; margin:0px 0%; min-height:300px; '><h4 style=\"text-align: center;\">Fitting the Motor\/Gearbox<\/h4>\r\n<p>Fitting the motor and gearbox in place was not too difficult. I made slots in the existing \"bearings\" that held the rear axle in placed and drilled out the rear screw hole that held the body to the chassis. The body of the motor would then sit in this enlarged hole and the gearbox would sit between the chassis rails. The wheels needed sleeving to fit the smaller diameter axles on the gearbox.<\/p>\r\n<p><img decoding=\"async\" class=\"aligncenter wp-image-2178 size-full\" src=\"https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/IMG_9126-2-scaled.jpg\" alt=\"IMG_9126 2\" width=\"2560\" height=\"1349\" srcset=\"https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/IMG_9126-2-scaled.jpg 2560w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/IMG_9126-2-300x158.jpg 300w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/IMG_9126-2-1024x540.jpg 1024w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/IMG_9126-2-768x405.jpg 768w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/IMG_9126-2-1536x809.jpg 1536w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/IMG_9126-2-2048x1079.jpg 2048w\" sizes=\"(max-width: 2560px) 100vw, 2560px\" \/><\/p>\r\n<p>The motor and gearbox in place, with a cage built around it to hold it in place. I plan to add some bearing to improve the running and make sure the axle is held square.<\/p><\/div>\n<div id='slider_2168_slide08' class='sa_hover_container' style='padding:5% 5%; margin:0px 0%; min-height:300px; '><h4 style=\"text-align: center;\">Wiring the Electronics<\/h4>\r\n<p>With all the components gathered it was simply a case of wiring the various parts together. Since I was using their breakout boards then it was a simple case of wiring the blocks together as shown.<\/p>\r\n<p><img decoding=\"async\" class=\"aligncenter wp-image-2184 size-full\" src=\"https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/Screenshot-2020-09-17-at-22.36.28.png\" alt=\"Screenshot 2020-09-17 at 22.36.28\" width=\"541\" height=\"405\" srcset=\"https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/Screenshot-2020-09-17-at-22.36.28.png 541w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/Screenshot-2020-09-17-at-22.36.28-300x225.png 300w\" sizes=\"(max-width: 541px) 100vw, 541px\" \/><\/p>\r\n<p>I had to remove the socket on the battery management board that was meant for the battery to connect to as my chosen battery had a different plug. This too was cut off and the wires soldered directly to the PCB. The battery management board and the WeMOS processor where soldered together to form a sandwich.<\/p><\/div>\n<div id='slider_2168_slide09' class='sa_hover_container' style='padding:5% 5%; margin:0px 0%; min-height:300px; '><h4 style=\"text-align: center;\">Fitting the boards<\/h4>\r\n<p>The boards where a good fit in the back of the Bedford. The two WeMOS board fit in the top of the load area, the H-Bridge edge on tucked down by the mounting pillar for the rear cover and the battery sitting on top of the motor.<\/p>\r\n<p><img decoding=\"async\" class=\"aligncenter wp-image-2185 size-full\" src=\"https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/IMG_0351-2-scaled.jpg\" alt=\"IMG_0351 2\" width=\"2560\" height=\"1920\" srcset=\"https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/IMG_0351-2-scaled.jpg 2560w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/IMG_0351-2-300x225.jpg 300w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/IMG_0351-2-1024x768.jpg 1024w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/IMG_0351-2-768x576.jpg 768w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/IMG_0351-2-1536x1152.jpg 1536w, https:\/\/www.missendenrailwaymodellers.org.uk\/wp-content\/uploads\/2020\/09\/IMG_0351-2-2048x1536.jpg 2048w\" sizes=\"(max-width: 2560px) 100vw, 2560px\" \/><\/p>\r\n<p>I have yet to add a charging socket and switch to turn it off, however this is enough for me to run it as a prototype.<\/p><\/div>\n<div id='slider_2168_slide10' class='sa_hover_container' style='padding:5% 5%; margin:0px 0%; min-height:300px; '><h4 style=\"text-align: center;\">Software<\/h4>\r\n<p>All that was left was the software, again this was produced on the principle of using building blocks. The ESP8266 is support by the Arduino programming environment, with lots of libraries available that make it easy to build up the software you want. A simple WiFi server was added that would allow an external computer to connect and send commands to the lorry. In this case you type F to go forwards and a speed, B to go backwards, again with a speed and S to stop. The Arduino environment has built in code to support PWM so this was simply a case of configuring the right outputs that had been wire to the H-Bridge.<\/p>\r\n<p>The lorry was then tested by connecting my laptop to the server running on the processing inside it and typing the commands on the keyboard. Later this will be replaced with another project that detects a particular DCC address and uses the speed setting to send commands to the lorry.<\/p><\/div>\n<\/div>\n<\/div>\n<script type='text\/javascript'>\n\tjQuery(document).ready(function() {\n\t\tjQuery('#slider_2168').owlCarousel({\n\t\t\titems : 1,\n\t\t\tsmartSpeed : 200,\n\t\t\tautoplay : true,\n\t\t\tautoplayTimeout : 5000,\n\t\t\tautoplayHoverPause : true,\n\t\t\tsmartSpeed : 200,\n\t\t\tfluidSpeed : 200,\n\t\t\tautoplaySpeed : 200,\n\t\t\tnavSpeed : 200,\n\t\t\tdotsSpeed : 200,\n\t\t\tloop : false,\n\t\t\tnav : true,\n\t\t\tnavText : ['Previous','Next'],\n\t\t\tdots : true,\n\t\t\tresponsiveRefreshRate : 200,\n\t\t\tslideBy : 1,\n\t\t\tmergeFit : true,\n\t\t\tautoHeight : true,\n\t\t\tmouseDrag : true,\n\t\t\ttouchDrag : true\n\t\t});\n\t\tjQuery('#slider_2168').css('visibility', 'visible');\n\t\tvar owl_goto = jQuery('#slider_2168');\n\t\tjQuery('.slider_2168_goto1').click(function(event){\n\t\t\towl_goto.trigger('to.owl.carousel', 0);\n\t\t});\n\t\tjQuery('.slider_2168_goto2').click(function(event){\n\t\t\towl_goto.trigger('to.owl.carousel', 1);\n\t\t});\n\t\tjQuery('.slider_2168_goto3').click(function(event){\n\t\t\towl_goto.trigger('to.owl.carousel', 2);\n\t\t});\n\t\tjQuery('.slider_2168_goto4').click(function(event){\n\t\t\towl_goto.trigger('to.owl.carousel', 3);\n\t\t});\n\t\tjQuery('.slider_2168_goto5').click(function(event){\n\t\t\towl_goto.trigger('to.owl.carousel', 4);\n\t\t});\n\t\tjQuery('.slider_2168_goto6').click(function(event){\n\t\t\towl_goto.trigger('to.owl.carousel', 5);\n\t\t});\n\t\tjQuery('.slider_2168_goto7').click(function(event){\n\t\t\towl_goto.trigger('to.owl.carousel', 6);\n\t\t});\n\t\tjQuery('.slider_2168_goto8').click(function(event){\n\t\t\towl_goto.trigger('to.owl.carousel', 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data-attributes='{&quot;align&quot;:&quot;&quot;,&quot;options&quot;:{&quot;controls&quot;:[],&quot;autoPlay&quot;:false,&quot;clickToPlay&quot;:false,&quot;muted&quot;:false,&quot;volume&quot;:0.5,&quot;seekTime&quot;:10,&quot;repeat&quot;:false,&quot;isAutoNextVideo&quot;:false,&quot;toolTip&quot;:false,&quot;isControl&quot;:true,&quot;shadowControl&quot;:true},&quot;videos&quot;:[{&quot;src&quot;:&quot;https:\\\/\\\/www.missendenrailwaymodellers.org.uk\\\/wp-content\\\/uploads\\\/2020\\\/09\\\/IMG_1920.mp4&quot;,&quot;title&quot;:&quot;type your video title here&quot;,&quot;poster&quot;:&quot;&quot;,&quot;description&quot;:&quot;Don\\u2019t forget to like, comment, and subscribe for more fun 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Arduinos &amp; Model Railways<\/a><\/p>\n","protected":false},"excerpt":{"rendered":"<p>A prototype project to create a WiFi controlled Bedford QLD lorry in 4mm scale. \u00a0 The prototype in action Back to Arduinos &amp; Model Railways<\/p>\n","protected":false},"author":1,"featured_media":0,"parent":0,"menu_order":0,"comment_status":"closed","ping_status":"closed","template":"","meta":{"pgc_sgb_lightbox_settings":"","slim_seo":{"title":"Virtual Missenden - WiFi Controlled Bedford - Missenden Railway 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